head resurfacing, deck heights and gasket sizing.
all may not be lost with my fully worked sr20ve head. by that i mean it can be returned back to 86 fairly easy and fairly cheaply.
here are some pics.
thats pics of the port work and port matching and the smothing of the valve guids to increase flow/velocity, i dont have any pics of the worked bowls. the head also recieved fully hand lapped valves.
we all know what a stock combustion chamber/deck looks like. i was under the impression when the machinest milled it out to 90mm it was similiar to what mazworx or head games would do to a head. quite simply i recieved the complete opposite. either way it worked and im glad thats all they did and heres why.
you can see here how the pistons stuck out of the block, this was la sleeves decking the head with out the timing cover (even though i told them too and included a brand new oil pump from gregv bolted to the block) forcing me to have the deck re-decked a second time with the timing cover.
i figured the thick mazworx headgasket would compinsate for this, i figured wrong. first time around the ends the outer edges hit the deck of the head head and also the upper most corners kissed the inside of the combustion chamber. motor was disassembled and the head was then milled out to 90mm so the outer edges of the pistons wouldnt touch the head and some material taken out of the upper inside of the chambers. the second time around they did not touch, and the motor ran for atleast 800miles before i hit the dyno.
heres a pic of what the machinest did.
you can clearly see here all they did was mill a 90mm circle step about .028 of an inch deep out of the deck matching the mazworx 90mm gasket.
heres a pic of a .026 feeler gauge, its a bit small and if i had to take a guess .028 would be dead flush as .030 is to much.
so basically if i mill whatever needs to be taken off .027-.029 ill be back to a perfectly square 86mm combustion chamber.
id then have to figure out what size mm head gaskets in 86 or 87mm are offered to compensate for the orginal deck of the head and the .028ish of an inch they took out. say run the thickest gasket avaliable or whatever.
then figure out if you'd wich i imagine you'd have still have plenty of piston to valve clearance on off the shelf pistons, if not you could always mill the pockets down some. regardless if i ever decide to build a ve of any sorts agian id have the motor clayed.
id just like to hear some feed back, and possibly some of your guys views and info on this. if im correct in thinking what i am, and if its possible with the use of the right head gasket etc.
what a nightmare this whole 2.4 thing was but im glad it seems the head is still salvagable it cost me some really good coin and i knew it would help me obtain my goal.
stratton.
here are some pics.
thats pics of the port work and port matching and the smothing of the valve guids to increase flow/velocity, i dont have any pics of the worked bowls. the head also recieved fully hand lapped valves.
we all know what a stock combustion chamber/deck looks like. i was under the impression when the machinest milled it out to 90mm it was similiar to what mazworx or head games would do to a head. quite simply i recieved the complete opposite. either way it worked and im glad thats all they did and heres why.
you can see here how the pistons stuck out of the block, this was la sleeves decking the head with out the timing cover (even though i told them too and included a brand new oil pump from gregv bolted to the block) forcing me to have the deck re-decked a second time with the timing cover.
i figured the thick mazworx headgasket would compinsate for this, i figured wrong. first time around the ends the outer edges hit the deck of the head head and also the upper most corners kissed the inside of the combustion chamber. motor was disassembled and the head was then milled out to 90mm so the outer edges of the pistons wouldnt touch the head and some material taken out of the upper inside of the chambers. the second time around they did not touch, and the motor ran for atleast 800miles before i hit the dyno.
heres a pic of what the machinest did.
you can clearly see here all they did was mill a 90mm circle step about .028 of an inch deep out of the deck matching the mazworx 90mm gasket.
heres a pic of a .026 feeler gauge, its a bit small and if i had to take a guess .028 would be dead flush as .030 is to much.
so basically if i mill whatever needs to be taken off .027-.029 ill be back to a perfectly square 86mm combustion chamber.
id then have to figure out what size mm head gaskets in 86 or 87mm are offered to compensate for the orginal deck of the head and the .028ish of an inch they took out. say run the thickest gasket avaliable or whatever.
then figure out if you'd wich i imagine you'd have still have plenty of piston to valve clearance on off the shelf pistons, if not you could always mill the pockets down some. regardless if i ever decide to build a ve of any sorts agian id have the motor clayed.
id just like to hear some feed back, and possibly some of your guys views and info on this. if im correct in thinking what i am, and if its possible with the use of the right head gasket etc.
what a nightmare this whole 2.4 thing was but im glad it seems the head is still salvagable it cost me some really good coin and i knew it would help me obtain my goal.
stratton.