You guys has been busy tonight.. But so have I...
Okay.. to your suggestions..
I was thinking that anywhere on the O2 sensor would ground the thing.. Wrong!! Attaching grounds to anywhere but the screw threads only gave about a 2% improvement. But, grounds to the threads makes anywhere from 30-34% improvement. So, attaching a ground to anywhere but between the header and the washers was useless...
Now, the strap is to thick to fit without causing a leak. So, you could rig-up something with a thin ring an attach that someway to the strap. But, with the heat and vibrations, Im not sure that would last very long. So, looked at my original plan again.
Grounding the header. Attached one end of the Grounding strap to a chassis bolt and the other end to the header. Testing at different locations on the header: Under the header bolt, under the AIV bung, clamped to the front surface, and clamped wedged between the pipes. All gave me only a 9-10% improvement with the bung giving the 10% and
believe it or not, the header bolt being the worst. I was really surprised by those results; especially the header bolts.
Making the Header Connection. Next, I cut the grounding strap in half and also split the cut end about 3 inches in the middle. Now, the cable can be split and placed between the Header/Downpipe joint. For this test, I decided
not to break the seal and cause an exhaust leak... So, I put a hole in each of ribbon ends for the bolts and bolted it down between the washer and flange on both sides. The test result was a respectable 26% improvement.
Making the Cat Connection. Then, I took the other half of the grounding strap and did the exact same thing at the Cat by attaching between the bolt head and cat flange on both sides. The test results gave me a total improvement of 38% which is great!!
. Although its not in the 40% range, I think its close enough...
I took the car for a short ride with the Datascan hooked up.. The O2 sensor is performing much better at low rpms.
Tomorrow, I will drive this car to work with the Datascan connected and see if rush-traffic bogging still exists or have improved. My idle still sucks but Im too tired tonight to put in
timing mode and make the necessary idle adjustments & timing checks.
So, it appears that the first round of testing has been a success thusfar..
Im going to pickup another strap tomorrow for more testing.
Cautious jubilation!!